Indonesia’s National Transportation Safety Committee (KNKT) sub-committee head for air accidents, Nurcahyo Utomo, holds a model airplane while speaking next to deputy chief of KNKT Haryo Satmiko during a news conference on its investigation into a Lion Air plane crash last month, in Jakarta, Indonesia. [REUTERS]
A Lion Air jet that crashed into the sea off Indonesia last month was not in an airworthy condition on its second-to-last flight, when pilots experienced similar problems to those on its doomed last journey, investigators said on Wednesday.
Contact with the Boeing 737 MAX jet was lost 13 minutes after it took off on October 29 from the capital, Jakarta, heading north to the tin-mining town of Pangkal Pinang.
In a preliminary report, Indonesia’s transport safety committee (KNKT) focused on the airline’s maintenance practices and pilot training and a Boeing anti-stall system but did not give a cause for the crash that killed all 189 people on board.
ALSO READ: 12 years left to limit climate change catastrophe, UN warns
The report unveiled fresh details of efforts by pilots to steady the jet as they reported a “flight control problem”, including the captain’s last words to air traffic control asking to be cleared to “five thou” or 5,000 feet.
Information retrieved from the flight data recorder showed the “stick shaker” was vibrating the captain’s controls, warning of a stall throughout most of the flight. The captain was using his controls to bring the plane’s nose up, but an automated anti-stall system was pushing it down.
Pilots flying the same plane a day earlier had experienced a similar problem, en route from Denpasar, Bali to Jakarta, until they used switches to shut off the system and used manual controls to fly and stabilize the plane, KNKT said.
“The flight from Denpasar to Jakarta experienced stick shaker activation during the takeoff rotation and remained active throughout the flight,” the committee said.
“This condition is considered as un-airworthy condition” and the flight should have been “discontinued”.
The pilots of that flight reported problems to Lion Air’s maintenance team, which checked the jet and cleared it for take-off the next morning.
Former Boeing flight control engineer Peter Lemme said stick shaker activation was “very distracting and unnerving”.
“It’s not something you ever want to have happen as a pilot,” he said.
KNKT investigator Nurcahyo Utomo said the agency had not determined if the anti-stall system, which was not explained to pilots in manuals, was a contributing factor.
“We still don’t know yet, if it contributed or not,” he said in response to a question. “It is too early to conclude.”
In a statement, Boeing drew attention in detail to a list of airline maintenance actions set out in the report but stopped short of blaming ground workers or pilots for the accident Reuters reported.
"Drone show is something I'd always watched and admired. We've travelled to Singapore, Paris and…
“You must embrace openness, accountability and compassion in all your dealings, knowing fully that the…
Akpabio urged senators to recommit themselves to national service with integrity and patriotism, and to…
"In adopting this framework, Kano state indeed been the first state not only to adopting…
“The KASU-ASUU strike is unnecessary"
"It weakens Nigeria’s voice in regional and global trade negotiations, it denies informal traders the…
This website uses cookies.